30 Jul 2005 currentc   » (Journeyer)

Finally got around to my robot again. Found a problem with the code while tweaking the speed settings for the servo motors. I had reversed all of my left/right ports while converting to the PIC, oops. I hope to get around to the new chassis this week.
Also added ramping to the servo speed/direction changes.

Latest blog entries     Older blog entries

Share this page